As of 16th of July, this site is delivered in a new layout, which *should* be mobile-compatible. The old theme’s backend has become too messy over time due to a lot of hacks I added. I still need to restore some parts of the old design though, so there will be some more change over the next few weeks.
Recently, the speedometer of my trusty old Volvo 850 station-wagon started acting up. Initially, it would just drop to zero intermittently at speed, then come back. Hard to notice if you only so much as glance at it every now and then. Over the last two weeks this got worse such that it would only very rarely do anything at all. My best guess for the cause would have been the speed sensor at the vehicle underside, but for mysterious reasons the odometer was still going at the normal pace. According to the instrument schematics, this should not be possible if the sensor were broken – same signal for both. Continue reading →
Getting a fitting transformer bobbin for ferrites is not easy under normal circumstances, but even more so for cores of unknown type. Usually, the dimensions follow a somewhat standardized pattern, but then your application might demand for separate winding chambers or mounting aids which are simply not available to the standard customer. So why not 3D print it?
The motivation is to use an old ferrite core for a high voltage lab supply. It will be driven far below its theoretical maximum spec as I only know it came from a ~50W power supply. My design (a flyback converter) requires a single winding in single-ended mode for the primary consisting of 23 turns, and a secondary of 235 turns capable of withstanding roughly 1kV. For winding I use standard enameled solid copper wire of unknown brand, which will probably not survive the full voltage. As a solution, I want to separate the secondary into 6 compartments of 40 turns each to reduce the maximum possible voltage between two neighboring wires to a maximum of 166V, which is well below the breakdown range. Without compartments, the left-to-right-to-left layer winding – which will occur somewhat naturally – may cause turns with extreme voltage difference to end up touching, leading to arcing sooner or later. To additionally strengthen the winding, a soaking resin could be applied.
Using the dimensions of the core as a base, some modeling in Tinkercad yielded this:
A few weeks ago a friend brought me an old subwoofer that was discarded as broken – a JAMO SUB-660, which is an 600W sub for home cinema with integrated amping. The sub receives pretty good reviews, so I set out to try and fix it. I have worked on quite a few power amps until now, but as fully switched designs like this rarely fail, it is always a challenge when they do.
Thin film electro-luminescent (TFEL) displays represent an interesting, if somewhat anachronistic display technology, now that we have high-contrast LCDs, plasma displays and of course OLEDs. The latter are actually closest to the principle of TFELs, and their primary optical advantage is identical: light-emitting pixels instead of backlighting, for maximum contrast. Where OLEDs use an organic polymer, which can be excited to emit visible light by applying an electric field, a TFEL does the same with an anorganic dielectric material like e.g., gallium arsenide (GaAs). The emitter pixels are sandwiched between two layers of transparent dielectric to insulate them from the transparent electrode grids on the front and back glass cover of the display panel. When a high-frequency current is applied, a current flows through the selected pixel and the emitter material lights up in a beautiful, saturated orange – in my opinion the most interesting aspect about this technology. Remember the old terminals with the amber CRT screen? Close! In contrast to OLEDs, EL displays are also able to tolerate much harsher environmental and mechanical conditions, which makes them ideal for applications in heavy machinery – or living room gadgets, when they are retired. Continue reading →
Some time ago, a water softening device was installed in my home main water supply line. Such a device contains one or multiple gel capsules that act as ion exchangers, replacing calcium and magnesium in the fresh water supply with sodium. In regions with a rather hard water, this can save you a lot of trouble with maintenance of valves and the lifetime of water-consuming devices like washing machines and dishwashers.
For regulation, a conductivity sensor determines the hardness of the incoming water. After running through the gel exchanger, the residual hardness is assumed to be around 0.5 °dH which allows the mixing ratio of raw and processed water to be calculated. I won’t go further into details here, the bottom line is: It works like a charm, water is as soft as it needs to be. The device at hand is built by JUDO and is available in several configurations. Basic models contain a two-capsule exchanger for seamless switchover/regeneration cycles and an integrated electronic control unit for automatic regeneration of the gel. A more advanced “i-Soft plus” model is extended by a touchscreen user interface complete with LAN/WLAN network access. This enables monitoring through a specialized iPad application where the interested user can view total water consumption per day, week, month or year as well as change different system parameters. As a nice bonus, the plus unit has an integrated main line valve which is closed automatically whenever user-set time, volume or flow rate limits are exceeded. This already saved my ass once when a pipe became leaky inside a wall. Unfortunately, the exact protocol for communication with the device is not disclosed, which is where this story begins. Continue reading →
After quite some time, I am finally starting to check my 4002 signal generator in-depth. The first thing I want to do before really starting this project is to get a good idea of the system layout, hence the “part 0” thing above. I will link from here to the different components as I wriggle through the unit and check them. As there is no service documentation freely available, I will go deeper into critical parts of the circuit along the way.
This will also help me simplify things later when trying to figure out which line went where, if things go wrong.
Clock source (Decade stage)
Contained in the bottom RF block, consists of a styrofoam-encapsulated 10.000(00…) MHz oven-controlled precision oscillator and some clock distribution buffering. This part sources the main TTL clock which is also available on the backside ports as an instrument reference. The picture shows the whole top side of the module block, but the actual OCXO and distributor PCB are on the right.
There are three additional circuits in this module: The 10 MHz TTL buffering and switchover for external references, a 10.7 MHz IF generator (PLL+VCO+Mixer) and another phaselocked VCO for a derived widerange signal (49.3-70.7 MHz according to the marking) which is used to fine-tune the RF synthesis stage.
While working up some extra circuits for the spectrum analyzer, I managed to pick up an old signal generator from eBay.
I heard a lot of positive things about the German(actually French origin, please look at comments below. Thanks to Rohit for pointing this out!) brand “Schlumberger” before, even though there is no relation to any personal experiences with their equipment. Seems like they also ran some kind of subcompany outfit called “Solartron” or “Enertec” which would today sound more than fishy, what with all those copycat-brands out there. But when an auction came up for a reasonable price I decided to go for it after some short research on the net.
What I got was a Schlumberger 4002 signal generator. It ranges from 0.1 to 2160 MHz with 10-20 Hz tuning accuracy, selectable output amplitude from -138.9 dBm up to +13 dBm in 0.1 dB steps, auto-sweeping and several extras like an OCXO for stability, 20 dB of linear attenuation range without using the step attenuator, an internal modulator and IEC bus remote control. If you looked at the photo closely, you will have noticed that the frequency range is written as “0.1…1000/2160 MHz” on the front panel. The reason for this is the optional doubler module included in this instrument. If the module is installed and detected, the software switches over to extended range without any further changes. Else, 1000 MHz is as far as it goes. More detailed specs will follow as soon as I can decypher the bad scan of a manual page that cropped up on Google. Judging from the inventory labels on the backside, the device must have been used in the manufacturer’s own lab. Unfortunately I have not yet managed to find any service info even though the manuals seem to be sold sometimes, for rather terrible prices. Continue reading →
As I already mentioned, the highest priority fix is the input RF attenuator. To get access to this, the control panel must be taken out since the connector is placed at a slightly inconvenient place – the bottom of the motherboard. Unfortunately, right beneath this is the aluminum carrier plate that contains all the RF circuits consisting of semi-rigid coax and clunky metal-jacketed modules. I first unmounted the top, bottom and right side panels, which was an easy job:
Loosen the single screws at the back of top and bottom covers and pull them off towards the back.
Remove the two screws holding the carrying handle and pull off the side panel along with it.
Also remove the top and bottom plastic inlays from the front aluminum frame, these cover up the panel screws.
Remove all visible screws from the top of the frame that seem to belong to the right panel (should be 3) and also from the bottom (should be 2). Take care not to remove the 2 rightmost screws on the bottom, these hold the front connectors and are best left in.
Now pull the control panel right out.
If it sticks, the points to watch out for are the N-type RF connector and the PCB edge of the sweep time selector. Gentle pulling while wiggling the panel up and down some will bring it out. Remove all connectors from the backside. Don’t worry, the plugs can’t be interchanged. Set the panel on a flat surface, front side down (Fig. 1). Continue reading →